Kentucky Hydrocarbons/DPI

Performed preliminary engineering and cost estimating for expanding an existing 55 MMSCFD cryogenic gas plant to 65 MMSCFD and improving overall liquids recoveries. The new design achieves 95% propane recovery (15% increase plus product recovered meets more stringent specifications) and utilizes 4,000 Hp less than the original design at the lower throughput.

Recent Stories

Hydrogen Transition #1

There has been a lot of dialogue and discussion lately on transitioning to hydrogen from natural gas. Much of this discussion is centered on reusing

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Adding Value #26

Doing what we do best. When we are onsite we are always looking out for problems with control logic that is causing equipment problems. Here

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Adding Value #25

Quality control /assurance is sometime taken for granted. After all there is a minimum level of confidence that we expect in terms of quality from

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